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Nitrogen Monitoring of Big Hill Strategic Petroleum Reserve Cavern Wells

Bettin, Giorgia B.; Lord, David L.; Roberts, Barry L.; Rudeen, David K.

In the past two years three SPR caverns, BH103, BH107 and BH112, have been placed under long term nitrogen monitoring following anomalous pressure behavior. This report focuses on the behavior of these caverns while under nitrogen, utilizing the Sandia hydrostatic column model to define the theoretical behavior under tight (no leak) conditions. All six wells exhibited reproducible pressure cycles with a creep-driven nitrogen pressurization rate relative to brine of 0.7, a value consistent with the model prediction for no-leak behavior. No current evidence of a leak in any of the wells was found. The wells do show evidence of notable deformation at the caprock/salt interface that is increasing with time. Additionally, geomechanical simulations predict that the wells are at high risk of casing failure by year ~2024 due to deformation induced by accumulated creep and subsidence effects.

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2015 Strategic Petroleum Reserve Bayou Choctaw Well Integrity Grading Report

Roberts, Barry L.; Lord, David L.; Lord, Anna S.; Bettin, Giorgia B.; Park, Byoung P.; Rudeen, D.K.; Eldredge, L.L.; Wynn, K.; Checkai, D.; Osborne, G.; Moore, D.

This report summarizes the work performed in the prioritization of cavern access wells for remediation and monitoring at the Bayou Choctaw Strategic Petroleum Reserve site. The grading included consideration of all 15 wells at the Bayou Choctaw site, with each active well receiving a separate grade for remediation and monitoring. Numerous factors affecting well integrity were incorporated into the grading including casing survey results, cavern pressure history, results from geomechanical simulations, and site geologic factors. The factors and grading framework used here are the same as those used in developing similar well remediation and monitoring priorities at the Big Hill, Bryan Mound, and West Hackberry Strategic Petroleum Reserve Sites.

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SPR Hydrostatic Column Model Verification and Validation

Bettin, Giorgia B.; Lord, David L.; Rudeen, David K.

A Hydrostatic Column Model (HCM) was developed to help differentiate between normal "tight" well behavior and small-leak behavior under nitrogen for testing the pressure integrity of crude oil storage wells at the U.S. Strategic Petroleum Reserve. This effort was motivated by steady, yet distinct, pressure behavior of a series of Big Hill caverns that have been placed under nitrogen for extended period of time. This report describes the HCM model, its functional requirements, the model structure and the verification and validation process. Different modes of operation are also described, which illustrate how the software can be used to model extended nitrogen monitoring and Mechanical Integrity Tests by predicting wellhead pressures along with nitrogen interface movements. Model verification has shown that the program runs correctly and it is implemented as intended. The cavern BH101 long term nitrogen test was used to validate the model which showed very good agreement with measured data. This supports the claim that the model is, in fact, capturing the relevant physical phenomena and can be used to make accurate predictions of both wellhead pressure and interface movements.

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Literature Survey Concerning the Feasibility of Remedial Leach for Select Phase I Caverns

Weber, Paula D.; Flores, Karen A.; Lord, David L.

Bryan Mound 5 ( BM5 ) and West Hackberry 9 ( WH9 ) have the potential to create a significant amount of new storage space should the caverns be deemed "leach - ready". This study discusses the original drilling history of the caverns, surrounding geology, current stability, and, based on this culmination of data, makes a preliminary assessment of the leach potential for the cavern. The risks associated with leaching BM5 present substantial problems for the SPR . The odd shape and large amount of insoluble material make it difficult to de termine whether a targeted leach would have the desired effect and create useable ullage or further distort the shape with preferential leaching . T he likelihood of salt falls and damaged or severed casing string is significant . In addition, a targeted le ach would require the relocation of approximately 27 MMB of oil . Due to the abundance of unknown factors associated with this cavern, a targeted leach of BM5 is not recommended. A targeted leaching of the neck of WH 9 could potentially eliminate or diminis h the mid - cavern ledge result ing in a more stable cavern with a more favorable shape. A better understanding of the composition of the surrounding salt and a less complicated leaching history yields more confidence in the ability to successfully leach this region. A targeted leach of WH9 can be recommended upon the completion of a full leach plan with consideration of the impacts upon nearby caverns .

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2015 Strategic Petroleum Reserve West Hackberry Well Integrity Grading Report

Roberts, Barry L.; Lord, David L.; Lord, Anna S.; Bettin, Giorgia B.; Sobolik, Steven R.; Rudeen, David K.; Eldredge, Lisa L.; Wynn, Karen; Checkai, Dean; Osborne, Gerad; Moore, Darryl

This report summarizes the work performed in the prioritization of cavern access wells for remediation and monitoring at the West Hackberry Strategic Petroleum Reserve site. The grading included consideration of all 31 wells at the West Hackberry site, with each well receiving a separate grade for remediation and monitoring. Numerous factors affecting well integrity were incorporated into the grading including casing survey results, cavern pressure history, results from geomechanical simulations, and site geologic factors. The factors and grading framework used here are the same as those used in developing similar well remediation and monitoring priorities at the Big Hill and Bryan Mound Strategic Petroleum Reserve Sites.

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2014 Strategic Petroleum Reserve Bryan Mound Well Integrity Grading Report

Roberts, Barry L.; Lord, David L.; Lord, Anna S.; Bettin, Giorgia B.; Sobolik, Steven R.; Rudeen, David K.; Eldredge, Lisa L.; Wynn, Karen; Checkai, Dean; Osborne, Gerad; Moore, Darryl

This report summarizes the work performed in the prioritization of cavern access wells for remediation and monitoring at the Bryan Mound Strategic Petroleum Reserve site. The grading included consideration of all 47 wells at the Bryan Mound site, with each well receiving a separate grade for remediation and monitoring. Numerous factors affecting well integrity were incorporated into the grading including casing survey results, cavern pressure history, results from geomechanical simulations, and site geologic factors. The factors and grading framework used here are the same as those used in developing similar well remediation and monitoring priorities at the Big Hill Strategic Petroleum Reserve Site.

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Literature Survey of Crude Oil Properties Relevant to Handling and Fire Safety in Transport

Lord, David L.; Luketa, Anay L.; Wocken, Chad; Schlasner, Steve; Aulich, Ted; Allen, Ray; Rudeen, David K.

Several fiery rail accidents in 2013-2015 in the U.S. and Canada carrying crude oil produced from the Bakken region of North Dakota have raised questions at many levels on the safety of transporting this, and other types of crude oil, by rail. Sandia National Laboratories was commissioned by the U.S. Department of Energy to investigate the material properties of crude oils, and in particular the so-called "tight oils" like Bakken that comprise the majority of crude oil rail shipments in the U.S. at the current time. The current report is a literature survey of public sources of information on crude oil properties that have some bearing on the likelihood or severity of combustion events that may occur around spills associated with rail transport. The report also contains background information including a review of the notional "tight oil" field operating environment, as well a basic description of crude oils and potential combustion events in rail transport.

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Nitrogen Monitoring of West Hackberry 117 Cavern Wells (Revision 1)

Bettin, Giorgia B.; Lord, David L.

U.S. Strategic Petroleum Reserve (SPR) oil storage cavern West Hackberry 117 was tested under extended nitrogen monitoring following a successful mechanical integrity test in order to validate a newly developed hydrostatic column model to be used to differentiate between normal “tight” well behavior and small-leak behavior under nitrogen. High resolution wireline pressure and temperature data were collected during the test period and used in conjunction with the hydrostatic column model to predict the nitrogen/oil interface and the pressure along the entire fluid column from the bradenhead flange nominally at ground surface to bottom of brine pool. Results here and for other SPR caverns have shown that wells under long term nitrogen monitoring do not necessarily pressurize with a relative rate (PN2/Pbrine) of 1. The theoretical relative pressure rate depends on the well configuration, pressure and the location of the nitrogen-oil interface and varies from well to well. For the case of WH117 the predicted rates were 0.73 for well A and 0.92 for well B. The measured relative pressurization rate for well B was consistent with the model prediction, while well A rate was found to be between 0.58-0.68. A number of possible reasons for the discrepancy between the model and measured rates of well A are possible. These include modeling inaccuracy, measurement inaccuracy or the possibility of the presence of a very small leak (below the latest calculated minimum detectable leak rate).

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Nitrogen Monitoring of West Hackberry 117 Cavern Wells

Bettin, Giorgia B.; Lord, David L.

U.S. Strategic Petroleum Reserve (SPR) oil storage cavern West Hackberry 117 was tested under extended nitrogen monitoring following a successful mechanical integrity test in order to validate a newly developed hydrostatic column model to be used to differentiate between normal "tight" well behavior and small-leak behavior under nitrogen. High resolution wireline pressure and temperature data were collected during the test period and used in conjunction with the hydrostatic column model to predict the nitrogen/oil interface and the pressure along the entire fluid column from the bradenhead flange nominally at ground surface to bottom of brine pool. Results here and for other SPR caverns have shown that wells under long term nitrogen monitoring do not necessarily pressurize with a relative rate (P N2 /P brine) of 1. The theoretical relative pressure rate depends on the well configuration, pressure and the location of the nitrogen-oil interface and varies from well to well. For the case of WH117 the predicted rates were 0.73 for well A and 0.92 for well B. The measured relative pressurization rate for well B was consistent with the model prediction, while well A rate was found to be between 0.58-0.68. A number of possible reasons for the discrepancy between the model and measured rates of well A are possible. These include modeling inaccuracy, measurement inaccuracy or the possibility of the presence of a very small leak (below the latest calculated minimum detectable leak rate).

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SANSMIC Validation

Weber, Paula D.; Rudeen, David K.; Lord, David L.

SANSMIC is solution mining software that was developed and utilized by SNL in its role as geotechnical advisor to the US DOE SPR for planning purposes. Three SANSMIC leach modes - withdrawal, direct, and reverse leach - have been revalidated with multiple test cases for each mode. The withdrawal mode was validated using high quality data from recent leach activity while the direct and reverse modes utilized data from historical cavern completion reports. Withdrawal results compared very well with observed data, including the location and size of shelves due to string breaks with relative leached volume differences ranging from 6 - 10% and relative radius differences from 1.5 - 3%. Profile comparisons for the direct mode were very good with relative leached volume differences ranging from 6 - 12% and relative radius differences from 5 - 7%. First, second, and third reverse configurations were simulated in order to validate SANSMIC over a range of relative hanging string and OBI locations. The first-reverse was simulated reasonably well with relative leached volume differences ranging from 1 - 9% and relative radius differences from 5 - 12%. The second-reverse mode showed the largest discrepancies in leach profile. Leached volume differences ranged from 8 - 12% and relative radius differences from 1 - 10%. In the third-reverse, relative leached volume differences ranged from 10 - 13% and relative radius differences were %7E4 %. Comparisons to historical reports were quite good, indicating that SANSMIC is essentially the same as documented and validated in the early 1980's.

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2013 strategic petroleum reserve big hill well integrity grading report

Lord, David L.; Roberts, Barry L.; Lord, Anna S.; Bettin, Giorgia B.; Sobolik, Steven R.; Park, Byoung P.

This report summarizes the work performed in developing a framework for the prioritization of cavern access wells for remediation and monitoring at the Big Hill Strategic Petroleum Reserve site. This framework was then applied to all 28 wells at the Big Hill site with each well receiving a grade for remediation and monitoring. Numerous factors affecting well integrity were incorporated into the grading framework including casing survey results, cavern pressure history, results from geomechanical simulations, and site geologic factors. The framework was developed in a way as to be applicable to all four of the Strategic Petroleum Reserve sites.

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Results 26–50 of 70
Results 26–50 of 70